
Related Resource: USS West Virginia Report of Pearl Harbor Attack
| U.S. NAVY YARD | ||
| Pearl Harbor, T[erritory of]. H[awaii]. | ||
| C-L11-1/BB48/Ser.01161 | June 15, 1942 |
From: The Salvage Officer
To: The Commandant, Navy Yard, Pearl Harbor, T.H.
Subject: USS West Virginia, Report of Salvage
of.
| Reference: | a. Salvaging of the USS West Virginia - Report of progress, March 16, 1942 |
| b. Salvage Bulletin #38, May 26, 1942. | |
| c. Salvage Bulletin #40, May 30, 1942. | |
| d. Salvage Bulletin #42, June 5, 1942. |
5. The above scheme of salvage was carried out as planned,
but somewhat further than contemplated in the matter of weight
removals in order to reduce the draft sufficiently to get the
vessel in Drydock #1. The original intent was to place the vessel
in Drydock #2 (which has 42 feet of water over the blocks at mean
low water) as soon as the dock was vacated by the [USS] California.
However, the military situation required that Drydock #2 be kept
available, except for very short intervals, in order that major
vessels damaged in action could be expeditiously handled. For
this reason the progress of salvage operations in the later stages
called for every possible means to reduce the draft to permit
drydocking in #1, - even contemplating, if necessary, some delay
in docking in order to attain a suitable draft to accomplish this
end. This decision was made despite the fact that it was fully
recognized that the West Virginia was very vulnerable to
sinking or even capsizing in case of reflooding because of failure
of the large patch due either to injury from collision, air attack
by the enemy, or even weakening due to Teredo [a type of marine
worm that eats wood] attack.
6. Design of Cofferdam Patch: The Navy was very fortunate
to have had available at Pearl Harbor the personnel and equipment
of the Pacific Bridge Company, contractors for new drydocks, new
bomb-proof powerhouse, etc. This company is very experienced in
cofferdam work and has been quick to adapt their practices and
experience to ship salvage requirements. With the cooperation
of various officers of the Salvage Division of the Navy Yard,
the Pacific Bridge Company worked up the detailed design of the
cofferdam patches for the West Virginia. A print showing
the general design will be forwarded to the Department by the
Commandant of the Navy Yard together with progress photographs
of the installation of the patches. Suffice it to state here that
the patch is made up in sections of about 13½ feet long.
Each section is about 50 feet in height and is made up of steel,
wood and concrete. The patch extends down from above the existing
water line to below the turn of the bilge. At the bottom point
it takes a right-angled turn so that it extends under the bottom
and is pulled up snuggly against the bottom. The end sections
of each patch are shaped to fit in snuggly against the damaged
shell. The patch is planked vertically with four inch material.
The net clearance between the armor and the inside of the patch
is about eighteen inches.
7. In order to eliminate shoring below the armor belt each section
has three steel vertical strength members. These are twenty-four
inch "I" beams running vertically about twenty feet
to a point just above the lower edge of the armor belt. On each
beam a bracket is welded and this bracket takes up on the underside
of the armor belt to take the upward thrust. There are ten wooden
strength members (wales) running fore and aft; these are 12"
X 14" timbers. These members are shored directly to the armor
on four foot six inch centers and above the armor to special steel
members resting on the armor belt.
8. Installation of Sections of Patches: The thirteen and
one half foot sections of the cofferdam patches were installed
once at a time on a schedule calling for one to be installed each
day. Slight negative buoyancy was obtained by placing a lead weight
in an angle bar frame attached to the outside near the bottom
of each section. This lead weight was removed when the section
was in place and used for the next section. All of the installation
work was handled with the assistance of the Pacific Bridge Company
divers, who did a masterful job of properly securing the sections
and subsequently making them relatively watertight.
9. The sections were secured to the hull by means of four horizontal
rows of steel hook bolts. Holes were burned into the hull with
an underwater gas torch for insertion of the bolts. The outer
end was passed through the patch structure and was drawn up snug
against the side by large butterfly nuts on the threaded outer
ends of the bolts. Proper distancing of each section from the
hull was maintained by the required structural shoring between
the hull and the wales of the section. Many of these shores (about
18 to 24 inches long) took up against the armor belt. These shores
varied inasmuch as the armor belt had been displaced as much as
fourteen inches from the original molded lines. Installing the
patch in relatively narrow sections (eleven joints in the large
patch) allowed the patch to follow both the lines of the ship
and curvature due to damage.
10. The armor belt was found to be badly askew but nevertheless
furnished excellent backing for shores. The chief difficulty in
shoring was to find suitable structure above the armor belt in
the midship area to shore against, - this for the reason that
all of the hull plating in the midship area above the armor belt
was missing or badly damaged. Shell plating that had been blown
out was removed previously by underwater cutting. An ingenious
scheme for shoring in this area was devised by setting ten inch
"H" beams vertically on end on top of the armor with
the lower end of the beam kept flush with the outer edge of the
armor by means of heavy angle bars which were welded to the "H"
beams but not to the armor. A hook bolt was fastened by divers
back of the armor. Above the water's edge the "H" beams
were backed by steel shapes which acted as struts between the
"H" beams and the structure of the ship. These vertical
members were tied together fore and aft by welded angles and channels.
When thus secured and spaced about every eight feet they furnished
a very substantial means against which to shore sections of the
patch to take the pressure as the water was pumped down.
11. The joints between the patches were made tight by using old
rubber hoses for gaskets and by drawing up the adjoining sections
by means of threaded bolts run though lugs on each section. These
were spaced vertically about every three feet.
12. Use of Concrete in the Patches: The forward patch consisted
of three sections and the after patch of eleven sections. After
these sections were all installed, the next operation was the
pouring of concrete, which was required to seal off the patch
along the bottom and take the bottom reaction of the steel structural
members and at each end. The concrete was of a rich mixture (about
one cement to three and one half aggregate) and was mixed on a
barge on which had been installed a contractor's cement mixing
plant. The crawler crane which was also on the barge handled the
two yard buckets to transfer the concrete from the mixer to the
hopper feeding down into the patch. Concrete was poured, of course,
underwater by the Tremie process used by the contractor in drydock
construction; ten inch Tremie pipes were placed at about ten foot
intervals. The concrete was installed about four feet deep along
the bottom of the patch for its whole length and the ends of the
patch had a fore and aft thickness of four feet. The total amount
of concrete used in both patches was 325 cubic yards or about
650 tons.
13. In order to take the weight of the sections in drydock after
the water had been pumped down there were two 1-¼"
steel rods running vertically from each twenty-four inch "I"
beam (six rods for each section) at the bottom of the patch to
an angle iron welded between the vertical "H" beams
or to the ship's plating where it was intact. In order to provide
access for divers into the patch, doors were fitted, - one on
the three section patch and four on the eleven section patch.
After the concrete was poured and all shoring completed the doors
were secured.
14. Unwatering of the Ship: As in the case of the [USS]
California, the pump capacity which was installed was more
than adequate for the estimated inflow of water. The 440 volt
electric Pomona and Peerless deep-well pumps (10") and several
Jaeger 10" gasoline pumps were used, a total of nine. Two
deep-well pumps were installed in the large patch and one in the
small patch. In the later stages these were changed from electric
to diesel driven in order to have them operative on the trip to
the drydock.
15. Before the patches were installed considerable pumping was
done to circulate water through the ship for the purpose of removing
water long stagnant, - together with gas (H2S) contained therein.
All main watertight doors and hatches were opened in order to
insure free flow of water throughout the main spaces of the ship.
Also, a number of the pump suctions were set at low levels, in
trunks and other areas to which various compartments could be
drained. For instance, one deep-well suction was sett in D-117
through a hole burned through the first platform deck with an
underwater cutting torch. Drainage holes were burned through the
shaft alley bulkheads so that water from the boiler rooms and
other spaces could drain to the pump through the main drain manifolds.
16. Two stages of pumping were considered; first to unwater the
third deck by mass pumping and second to unwater individual compartments
either by direct pumping or through the ship's drainage systems.
Due to extensive damage to the third deck bulkheads in way of
the patches there was little if any watertight integrity down
to the third deck and the water in the patch had to be lowered
to this level before the third deck could be made dry.
17. As soon as the patches were considered reasonably tight the
unwatering of the ship was commenced, - May 12, 1942. The water
level within the ship and patches was rapidly reduced four or
five feet, but at this point the inflow almost equaled the pumping
capacity. This difference in head, however, showed up at points
of inflow, and it was a matter of a day or two for the divers
to find the larger leaks in the patches, through open ports, etc.,
and to remedy them. Continuous effort was devoted to improving
the watertightness of the patches and of stopping off leaks through
holes in the ship. Much of the leakage was not in the patch itself
but through damage in the areas contiguous to the patches, open
seams, shrapnel holes, loose rivets, scuppers, etc. As the points
of inflow were taken care of the water level within the ship was
reduced rapidly and the ship came afloat on 17 May 1942.
18. After the third deck was uncovered a number of small Barns
(3") pumps were connected up to the various storerooms and
small compartments. Pumping out of the lower compartments continued
unabated until the ship was ready for drydock. The unwatering
of these lower spaces has proved most difficult and slows the
unwatering of the ship, principally for the reason that the spaces
cannot be drained to other areas, and small pump suction must
be brought to each individual compartment.
19. Removal of Oil: There was a very large quantity of free oil
within the West Virginia and early steps were taken to
remove the same prior to reducing the water level. A floating
Wheeler System took suction in various places throughout the upper
decks and spaces on the West Virginia and was operated
continuously for four or five weeks before the ship pumping was
commenced. This resulted in removal of most of the fuel oil in
the ship as a result of which there was considerably less oil
nuisance on the decks and bulkheads as the ship was pumped down.
In the later stages of pumping an additional Wheeler System was
installed on the quarter deck to assist in the removal of oil
from lower spaces such as engine room bilges, boiler rooms, etc.
About 40,000 gallons of loose oil were removed by the Wheeler
System.
20. During salvage work about 800,000 gallons of oil were removed
from the oil tanks of the ship. The oil from the tanks was pumped
into fuel oil barges by use of the West Virginia's fuel
oil transfer pumps operated by air. In many cases air pressure
was applied to the tops of the tanks in order to assist the pumps.
In order to keep the ship approximately on an even keel no oil
or water was removed from the starboard tanks or voids unless
a corresponding amount had been taken from the port side, in the
emptying of tanks and voids. When it became necessary to lessen
the draft of the ship to a point permitting the docking in Drydock
#1it was necessary to reduce the amount of oil or water in damaged
areas to the very minimum. The pumping arrangement was such that
spaces on the port side which were open to the sea through side
damage were drained outboard into the patches and picked up by
the pumps which took suction from near the bottom of the patches.
In order to reduce the water level in such spaces the pup suction
were finally set down to within about four inches of the concrete
in the bottom of the patches. Inasmuch as some flooding of tanks
and voids was through the bottom of the ship or through holes
in bulkheads near the tops of these spaces it was apparent that
such areas would not drain. In order to reduce their water level
a combination of air pressure and individual pumps was utilized.
The air pressure was used to force the water out of the holes
which permitted flooding through the bottom of the ship. Pump
suctions (3") were used to remove water which wold not drain
into the patches; air pressure was oftentimes used to assist the
pumps.
21. Hazard of Capsizing: Due to the fact that no drydock
was available when the ship was fully afloat there came to exist
a hazard that certain events might cause resinking of the ship
and possible capsizing. The possibility of capsizing in case of
failure of the large patch (which might occur in case of an air
attack) was clearly recognized. As the ship rose higher and higher
this condition was accentuated, due primarily to the fact that
the whole midship area of the port side above the armor belt was
entirely open, and the decks down to and including the second
deck were collapsed. Watertight doors and hatches in this area
were useless, and fore and aft of this area most of them were
required to be open for the passage of suction hoses, air hoses,
light leads, steam leads, etc. However, an air-raid bill was worked
up to insure that as many watertight doors and hatches as possible
would be closed in the event of such an emergency. Several other
precautions were taken, such as: (a) construction of two seam
patches and one section patch to be available on the crane barge
for placing over ruptures in the cofferdam patches, and (b) having
available for counterflooding eight to ten voids on the starboard
side with men assigned for the quick operation of sea valves.
Fortunately the air raid which might have occurred was stopped
off Midway and none of the precautions were actually necessary.
22. Emptying of Double Bottom Tanks, etc: Fresh water tanks, innerbottom
tanks, etc., were emptied by the use of ship's pumps operated
by air. It was the general rule to operate ship's pumps and ship's
facilities to the maximum possible extent with air in lieu of
steam.
23. Removal of Ammunition: All ammunition was removed from
the ship and most of the ordnance stores. The ship's force handled
the removal of ammunition unusually well. Sixteen- inch shells
were hoisted by the barge crane through the top of the turrets
in the case of the upper stowages; the shells from the handling
rooms were hoisted through the ammunition handling hatches. The
five-inch shells were brought up by the regular ammunition hoists
operated by air drills (corner type); in the later stages 5"/25
shells [shells for secondary battery guns with bore size of five
inches and in which the bore was 25 calibers long, viz., 125 inches]
were passed by hand. Powder and ordnance gear were hoisted through
various hatches by means of small air driven winches (tuggers)
installed on the topside.
24. Removal of Meat: Considerable apprehension was felt
over handling approximately 70 tons of meat which was assumed
to be in a bad state of decomposition. Some thought was given
to pumping water at high pressure through the meat rooms so that
the meat would be taken up by the water and discharged through
a 10" pipe over the side. A modified arrangement of this
kind was tried and although it did not prove wholly effective
it reduced the odor (a disagreeable part of the task) to a point
which was quite acceptable. The meat itself after being flushed
with water had the appearance of ashes and its texture shreddy.
This was shoveled up and placed in ten gallon cans (gas mask containers)
and hoisted by air winches to the quarter deck and dumped into
the garbage lighter alongside. All in all the removal of decayed
meat and dairy products was not really so disagreeable as was
anticipated.
25. Removal of Stores: Small air driven winches were used
to hoist canned goods, flour, etc., to the weather decks. These
materials were then loaded on wheel barrows and dumped into the
lighters alongside. The canteen stores and flour were most unpleasant
to handle and it was necessary for the men working in the storerooms
involved to wear protective masks. The canned goods were generally
in a bad state due to the corrosion of the cans which in many
instances permitted deterioration of the contents and the generation
of gas and disagreeable odors.
26. Toxic Gases: As in the case of the [USS] California
and the [USS] Nevada there existed a considerable hazard
due to the presence of toxic gases. The principal offender was
hydrogen sulphide, H2S (sewer gas), which was generated in the
contaminated stagnant water. It was found that the most serious
gas concentrations occurred in storerooms containing a large amount
of paper or where there was a large quantity of cardboard containers.
Numerous cases of oxygen deficiency were found and some cases
of carbon monoxide.
27. Precautions Taken Against Toxic Gases: A systematic
procedure for testing for toxic gas was employed, and was in charge
of Lieutenant Commander C. M. Parker (MC), USN, who is a specialist
in industrial gas hazards. A large bulletin board was kept marked
up to indicate to personnel which compartments were safe and which
should not be entered without proper mask protection. Although
extraordinarily high concentrations of gases were found on the
West Virginia (two hundred thousand parts to one million)
there were no persons overcome by gas. If the concentration reached
the points of 20 parts in a million, as shown by detectors, the
space was considered unsafe except with a rescue breathing apparatus
or suitable face plate with air lead.
28. Ventilation: In order to combat the gas hazard and
to permit work to go on with the least possible delay there were
installed a large number of exhaust ventilation units. As the
water was pumped down these were connected up to the ship's ventilation
pipes so that all parts of the ship could be reached and the toxic
gases withdrawn.
29. Recovery of Bodies: During the salvage operations sixty-six
bodies were recovered from the West Virginia. These were
found widely scattered throughout the ship. In most cases they
were in an advanced state of decomposition, and considerably dismembered.
As in the case of the California the bodies were handled
in heavy canvas bags made for the purpose; when drawn tight at
the top for closing the odors emitted were negligible. By this
means the bodies were removed from the ship at various times almost
unnoticed by the working parties on board.
30. There were evidences that some of the men had lived for considerable
period and finally succumbed due to lack of oxygen. In the after
engine room, several bodies were found lying on top of the steam
pipes, which areas were probably within the air bubble existing
in that flooded space.
31. Three bodies were found on the lower shelf of storeroom A-111
clad in blues and jerseys. This storeroom was open to fresh water
pump room, A-109, which presumably was the battle station assigned
to these men. The emergency rations at this station had been consumed
and a manhole to the fresh water tanks below the pumps had been
removed. A calendar which was found in this compartment had an
"X" marked on each date from December 7, 1941 to December
23, 1941 inclusive.
32. Removal of Personal Effects and Trash: All personal
effects, furniture, etc., were thoroughly soaked with fuel oil
and in some cases had been burned. As in previous salvage jobs
it was necessary to remove all such material either as scrap or
for reconditioning. The West Virginia force handled the
removal of trash in a very expeditious manner by using wheel barrows
on the lower decks. They attached shackles to four points on the
barrows so that hooks from the hoist line could pick up the wheel
barrows and raise same to the weather deck through open hatches.
From this point the barrows could be wheeled on to trash lighters
and dumped.
33. Condition of Main and Auxiliary Machinery: The condition
of the main propulsion plant and the auxiliary machinery throughout
the ship was approximately the same as in the case of the California.
There was more free oil removed from the West Virginia
than from other salvaged vessels and as a result there was less
deposited on the decks, bulkheads, electrical machinery, etc.
The program of removing the electric motors and sending same to
the Navy Yard for reconditioning locally or elsewhere was proceeded
with as the water level was reduced. Yard workmen were available
in large numbers to assist in the removal and reconditioning of
mechanical machinery, machine tools, instruments, etc. This fact
insures that a larger percentage of the instruments and delicate
installations such as gyros, fire control equipment in plot, etc.,
have been subjected to less corrosion than in the case of the
California. "Tectyl" was used freely as a preventative
agent on mechanical parts of the fire control instruments, pumps,
turbines, etc.
34. The main machinery spaces were well cleaned down before the
vessel was docked and preliminary steps were underway to disassemble
main generators and main motors. It appears certain that the job
of rewinding these units will get underway very soon and will
proceed at a good rate.
35. All in all, the condition of all mechanical machinery is good
to excellent, and it is anticipated that it can be reconditioned
100%. All electrical machinery requires rehabilitation and the
present decision is to rewind all vital items. It is expected
that the rewinding work will be done in part at the Navy Yard
here but mostly under contract on the West Coast.
36. Structural Damage: Pumping down of the drydock revealed the
full extent of the damage to the hull of the West Virginia.
The damage on the port side amidships from the turn of the bilge
to the boat deck, is so extensive as to beggar description. All
of the ship's structure in this area, including a number of the
armor plates, requires renewal. A detailed damage report will,
of course, be submitted by the Navy Yard, Pearl Harbor, but a
general listing of the damage appears pertinent to this Salvage
Report. The general damage is as follows:
37. I think that the causes and effects of the various aspects
of damage in the midship area of the West Virginia is a
matter for careful study, and any conclusions are pretty much
a matter of individual opinion. Based on the above it is my present
opinion that the West Virginia was struck by six torpedoes
and two large bombs, or by four torpedoes and four large bombs.
The torpedoes, it would appear were shallow running torpedoes,although
some of them may have struck when the ship was well listed over.
The maximum list attained by the ship was about twenty-eight degrees.
38. Damage from Fire: Very extensive damage was suffered from
fires which burned for nearly thirty hours. Most of the fire was
from oil floating on the surface of the water, both inside and
outside the ship. The water level on the inside was three or four
feet below the main deck on the starboard side and the fires on
the surface of the water there caused serious buckling of main
deck plating. In large part this will require renewal and/or straightening.
39. The direct contact of torpedo and/or bomb explosions against
the armor belt caused the third deck to absorb considerably more
energy than is usually the case in way of torpedo explosions.
As a result the damage to and on the third deck in the midship
area is very extensive. This damage extended to #5 torpedo bulkhead
which is pushed in as much as two feet in boiler rooms two and
four. Also, there is considerable buckling and failure of bulkhead
stiffeners, bracket, etc.
40. Extent of Structural Damage and Time to Repair: The time required
to make good the structural damage to the West Virginia
depends upon numerous considerations such as, availability of
material, number of structural trades available, handling of armor,
etc. Obviously the armor belt in way of the damage must be removed
and the whole structure from the shell to torpedo bulkhead #5
inclusive must be replaced in large part. It seems that five armor
plates are cracked and all or most of these may require renewal;
also, it may be found that some of the armor keyways of others
are broken open so as to require replacement of the armor plate.
The bottom of the ship under the turn of the bilge is rumpled
considerably and is pulled up in way of torpedo bulkhead #5. The
docking keel is pulled up by six to eight inches. It is not blown
out at any place and is damaged comparatively less than in the
case of the California.
41. With material and men available it would seem that the structural
job on the West Virginia would require some four to six
months. A large part of this work can be deferred until the vessel
reaches a mainland yard, especially most of the renewal and straightening
of main and upper decks. The time required for the steering gear
job is anybody's guess at this stage and depends primarily on
the delivery of new parts such as stern post, rudder stock, crosshead,
etc.
42. The Yard is being pressed to have the West Virginia
in condition to vacate the dock if emergency requires. It is likely
that the inner bulkheads can be made tight to permit refloating
of the vessel after a period of about three weeks in dock. Although
structural repairs can best be done in dock, it would be possible
to handle the work so that only the outer layers need be done
in dock and the inside layers competed thereafter. While this
would not be the most efficient way of doing the job it would
cut down the total drydock period to approximately ten to twelve
weeks.
43. Temporary Quarters on Ford Island: In order to house the West
Virginia's crew near their work and to avoid loss of considerable
time in boat transportation, a temporary barracks was constructed
on Ford Island. A walkway from the West Virginia to Ford
Island was carried on floats on the water. This arrangement paid
high dividends and permitted a very satisfactory arrangement for
handling the crew of the ship and added considerably to the morale
of the working organization.
44. Electrical PowerCompressed AirSteam: The electric power was
furnished to the ship through leads from Ford Island. Steam was
furnished by the tug ex-Navajo and piped through the ship
in temporary piping. Compressed air was generated by about six
large air compressors on the boat deck and on the main deck, and
distributed from an accumulator.
45. Personnel Assigned to the West Virginia: The officer
assigned as the principal assistant to the Salvage Officer was
Lieutenant Wilfred L. Painter, CEC-V(S), USNR, who had direct
charge of all aspects of the work including coordination with
the ship's complement. Prior to the completion of the California
salvage Lieutenant Emile C. Genereaux Jr., DV(S), USNR, was in
direct charge of the West Virginia work but due to his
assignment to the [USS] Plunger job he was relieved by
Lieutenant Painter. Other officers assigned were as follows:
46. The performances of the above officers in all aspects of
the work from design of cofferdam patches to installation of same,
operation of pumps, removal of wreckage, removal of oil and water,
etc., was of the highest order. They carried on the work with
outstanding devotion to duty, enthusiasm, and high courage in
the face of unusual hazard from toxic gases, dangerous wreckage,
etc. I have recommended letters of commendation for Lieutenant
W. L. Painter, Lieutenant (jg) J. W. Darrock and Lieutenant (jg)
E. H. Liedstrand in view of their excellent work throughout the
whole period of actual salvage operations.
47. The great success attained in salvaging the badly damaged
West Virginia is in great part due to the personnel, experience
and excellent cooperation of the Pacific Bridge Company, contractor
for the new drydocks at this Navy Yard. Their work on design,
installation, and upkeep of the cofferdam patches was of inestimable
value. The underwater work performed by their divers in the fitting,
attaching, and securing of the cofferdam patches was an outstanding
achievement in underwater work. Officers who viewed the work after
docking expressed astonishment and marveled at the immensity of
the achievement. I am preparing for the signature of the Commandant
a letter to the Pacific Bridge Company expressing the appreciation
of the Navy Yard for their fine work. This letter will make special
mention of those representatives of the company where were outstanding
in the West Virginia work, such as; the local manager Mr.
Jack Graham, the supervisor in direct charge of the West Virginia
work, Mr. Les Freeman, the rigging supervisor, Mr. Bert Rice,
the design superintendent Mr. Fred Crocker, and design assistant
Mr. James Foster.
48. The Pearl Harbor Repair and Salvage Unit rendered valuable
assistance in operation of pumps and in removing and reconditioning
certain auxiliary machinery. Due to the transfer of many of the
officers and a considerable number of the men from this area it
was not possible for this unit to assist in the same degree as
they did on the California.
49. The various shops of the Navy Yard assisted in their specialties
in the salvage work, especially in the operation of the air compressors
and ventilation blowers. The work on the ship would not have been
possible without the installation of a tremendous ventilation
system for the removal of toxic gases. Most of this work was performed
by Navy Yard workmen and coordinated by the Shop Superintendent's
office.
50. The officers and crew of the West Virginia turned out
a record of work and accomplishment which will probably never
be equaled. The Commanding Officer, Lieutenant Commander W. White,
USN, and the Ship's Superintendent, Lieutenant Commander L. J.
Knight Jr., USN, and many other officers were on the job at all
hours to do the part of the salvage work assigned to them and
to render assistance which might be required for any purpose.
Unfortunately the shortage of enlisted men which has recently
prevailed here, prevented the building up of the crew of the West
Virginia. The maximum number in the crew did not exceed three
hundred and seventy. Sixty of these were Marines, who assisted
in their traditional spirit and were always willing to do nothing
less than their share of the work, and then some. With the small
crew available the West Virginia work was carried along
rapidly so that before drydocking the removal of the larger part
of the wreckage and trash, all of the ammunition, and much of
the stores and provisions had been accomplished. I should mention
also, that the initiative and spirit of the West Virginia
resulted in the recommissioning of the officers' galley which
was operated continuously from April 27, 1942, to feed on board
the ship three meals a day to all of the ship's officers and crew.
I have prepared a letter for the Commandant's signature expressing
appreciation of the excellent co-operation and assistance rendered
by the officers and crew of the West Virginia in the salvage
of that ship.
51. The above is in general the story of the salvage of the West
Virginia, which may well be designated as a most difficult
salvage job successfully completed. All hands assigned to the
work performed their part intelligently, co-operatively and effectively.
A successful outcome was never in doubt.
| cc. | Comserfor. |
| Mgr. | |
| Prod. Off. | |
| Plann. Off. | |
| Shop Supt. |
| [signed] |
| H. N. WALLIN |